[1]何云腾,吴奇霖,陈三君,等. 定容管活塞式油气水多相流量计[J].油气井测试,2019,28(04):45-50.[doi:10.19680/j.cnki.2019.04.008]
 HE Yunteng,WU Qilin,CHEN Sanjun,et al. Pistontype oilgaswater multiphase flowmeter with constant volume tube[J].Well Testing,2019,28(04):45-50.[doi:10.19680/j.cnki.2019.04.008]
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 定容管活塞式油气水多相流量计()
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《油气井测试》[ISSN:1006-6977/CN:12-1485/TE]

卷:
28
期数:
2019年04期
页码:
45-50
栏目:
出版日期:
2019-08-25

文章信息/Info

Title:
 Pistontype oilgaswater multiphase flowmeter with constant volume tube
文章编号:
1004-4388(2019)04-0045-06
作者:
 何云腾1吴奇霖2陈三君2李东晖1吴辰3朱沫3
 1.中国科学院力学研究所 北京 100190
2.中海石油(中国)有限公司深圳分公司生产作业部 广东深圳 518067
3.中海油能源发展装备技术有限公司深圳分公司 广东深圳 518067
Author(s):
 HE Yunteng1 WU Qilin2 CHEN Sanjun2 LI Donghui1 WU Chen3 ZHU Mo3
1 . Institute of Mechanics, Chinese Academy Sciences, Beijing 100190, China
2. Department of Production, Shenzhen Branch of CNOOC Ltd., Shenzhen, Guangdong 518067, China
3. Shenzhen Branch, CNOOC Enertech Equipment Technology Co., Ltd, Shenzhen, Guangdong 518067, China
关键词:
 定容管 活塞 油气水多相流量计 相含率 体积流量 单井计量 油井采出液
Keywords:
 

constant volume tube piston oilgaswater multiphase flowmeter phase holdup volume flow single well

metering produced fluids of oil well

分类号:
TE353
DOI:
10.19680/j.cnki.2019.04.008
文献标志码:
B
摘要:
 

为验证定容管活塞式油气水多相流量计的计量精度及适用性,在XJ243平台和EP242平台上进行测试实验。受现场测试条件限制,将多相流

量计串联入测试管汇。8口单井实验结果表明,多相流量计计量液量和含水率测试与传统测试分离器计量和手工取样测含水的结果误差约±5%;与平台上现有传统计量

设备相比,能快速进行单井井口计量切换,且测试结果吻合度较好。该多相流量计现场环境友好,计量准确快速,可简化现场工艺流程,具有推广应用价值。

Abstract:
 

In order to verify the measurement accuracy and applicability of the pistontype oilgaswater multiphase

flowmeter with constant volume tube, test trials were carried out on XJ243 platform and EP242 platform. Due to the limitation of field test

conditions, multiphase flowmeters were connected in series to the test manifold. The test results of 8 single wells show that the error of liquid

volume and water content measured by the multiphase flowmeter was less than ±5% when compared with the results of traditional separator

measurement and manual sampling measurement. Compared with the existing traditional measurement equipment on the platform, the multiphase

flowmeter can quickly switch the metering of wellhead in single well, and the test results were in good agreement. The multiphase flowmeter was

environmentally friendly, accurate and fast in measurement, and can simplify the process flow on site. It has the values of popularization and

application.

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备注/Memo

备注/Memo:
 2018-08-30收稿,2019-05-20修回,2019-06-18接受,2019-08-20 网络版发表

中国科学院战略性先导科技专项(B类)“超常环境下系统力学问题研究与验证”(XDB22000000)、中国海洋石油总公司“十三五”重

大科技项目“海相砂岩油田‘双特高’开发后期提高采收率技术”(CNOOCKJ 135 ZDXM 22 LTD 03 SZ 2016)

何云腾,男,1989年出生,工程师,2013年毕业于南京工业大学应用化学系,现主要从事多相流检测技术原型机的测试

工作。电话:010-82544173,18614049261;Email:HYT@imech.ac.cn。通信地址:北京市海淀区北四环西路15号中国科学院力学研究所,邮政编码:100190。


更新日期/Last Update: 2019-09-03