[1]张士川,陈燕,雷鹏,等. 应用天然气密闭燃烧装置提高杨税务潜山气藏试气安全环保质量[J].油气井测试,2020,29(04):18-23.[doi:10.19680/j.cnki.1004-4388.2020.04.003]
 ZHANG Shichuan,CHEN Yan,LEI Peng,et al.Applying airtight combustion device for natural gas to improve the safety of gas testing and environmental quality in Yangshuiwu buried hill gas reservoir[J].Well Testing,2020,29(04):18-23.[doi:10.19680/j.cnki.1004-4388.2020.04.003]
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 应用天然气密闭燃烧装置提高杨税务潜山气藏试气安全环保质量()
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《油气井测试》[ISSN:1006-6977/CN:12-1485/TE]

卷:
29卷
期数:
2020年04期
页码:
18-23
栏目:
出版日期:
2020-08-25

文章信息/Info

Title:
Applying airtight combustion device for natural gas to improve the safety of gas testing and environmental quality in Yangshuiwu buried hill gas reservoir
文章编号:
1004-4388(2020)04-0018-06
作者:
张士川1陈燕1雷鹏1刘述忍1徐文光2尹后凤3
Author(s):
ZHANG Shichuan1 CHEN Yan1 LEI Peng1 LIU Shuren1 XU Wenguang2 YIN Houfeng3
1 .Well Testing Branch, CNPC Bohai Drilling Engineering Co., Ltd., Langfang, Hebei 065007, China
2.Petroleum Engineering General Contracting Branch, CNPC Bohai Drilling Engineering Co., Ltd., Xi′an, Shaanxi 710016, China
3.Huagang Gas Group Co., Ltd., CNPC Huabei Oilfield Branch, Renqiu, Hebei 062552, China
关键词:
 潜山气藏 试油 密闭燃烧 天然气 地面计量 自动控制系统 安全环保
Keywords:
 buried hill gas reservoir oil testing airtight combustion natural gas surface measurement automatic control system safety and environmental protection
分类号:
TE27
DOI:
10.19680/j.cnki.1004-4388.2020.04.003
文献标志码:
B
摘要:
 为保证杨税务潜山气藏在勘探过程中符合环保要求,研制了天然气密闭燃烧装置。通过结构设计和高温耐火材料选型,制造了燃烧装置的炉体,实现燃烧器的点火、供气、降温、送风、监测、自动化控制等功能,建立了完善的安全监测和保护系统;设计了天然气放喷、回收、密闭燃烧控压系统,并配套了相应的软件。经在华北油田杨税务潜山气藏6口天然气井试气放喷应用,有效降低了噪音、热辐射、光污染和有害气体排放, 各项指标均符合国家标准,具有明显的工程优势,可为石油勘探开发提供有力的技术支撑。
Abstract:
 In order to ensure that the exploration of Yangshuiwu buried hill gas reservoir meets environmental protection requirements, an airtight combustion device for natural gas was developed. Through structural design and selection of hightemperature refractory materials, the furnace body of the combustion device was manufactured to realize the functions of ignition, gas supply, cooling, air supply, monitoring, and automatic control of the burner. A complete safety monitoring and protection system was established. The pressure control system for natural gas relief, recycle, and airtight combustion was designed, and corresponding software was provided. The application of gas relief testing in 6 natural gas wells in the Yangshuiwu buried hill gas reservoir of Huabei Oilfield shows that the device can significantly reduce noise, heat radiation, light pollution and harmful gas emissions, and all indicators are in line with national standards. The device has obvious engineering advantages, and can provide strong technical support for petroleum exploration and development.

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备注/Memo

备注/Memo:
 2020-04-29收稿,2020-06-25修回,2020-07-01接受,2020-08-20网络版发表
中国石油集团渤海钻探工程有限公司科研项目“天然气密闭燃烧装置研究与应用”(2018Z32K)
张士川,男,1982年出生,工程师,2005年毕业于河北经贸大学计算机科学与技术专业,现从事油气井测试相关工作。电话:0317-2553898,15931606648;Email:zhang_sc@cnpc.com.cn。通信地址:河北省廊坊市广阳区万庄石油基地油气井测试公司,邮政编码:065007。
更新日期/Last Update: 2020-09-21