[1]刘飞,张凯权,朱永国,等. 过油管桥塞封堵工艺改进[J].油气井测试,2020,29(04):35-39.[doi:10.19680/j.cnki.1004-4388.2020.04.006]
 LIU Fei,ZHANG Kaiquan,ZHU Yongguo,et al. Plugging technology improvement of through tubing bridge plug[J].Well Testing,2020,29(04):35-39.[doi:10.19680/j.cnki.1004-4388.2020.04.006]
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 过油管桥塞封堵工艺改进()
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《油气井测试》[ISSN:1006-6977/CN:12-1485/TE]

卷:
29卷
期数:
2020年04期
页码:
35-39
栏目:
出版日期:
2020-08-25

文章信息/Info

Title:
 Plugging technology improvement of through tubing bridge plug
文章编号:
1004-4388(2020)04-0035-05
作者:
 刘飞1张凯权2朱永国2关健2马礼2王吉飞2
 1.中国石油集团渤海钻探工程有限公司井下作业分公司 河北任丘 062552
2.中国石油集团渤海钻探工程有限公司油气井测试分公司 河北廊坊 065007
Author(s):
 LIU Fei1 ZHANG Kaiquan2 ZHU Yongguo2 GUAN Jian2 MA Li2 WANG Jifei2
 1. Downhole Operating Branch, CNPC Bohai Drilling Engineering Company, Renqiu, Hebei 062552, China
2. Well Testing Branch, CNPC Bohai Drilling and Engineering Co., Ltd., Langfang, Hebei 065007, China
关键词:
 完井 过油管 桥塞 水泥塞 封堵 套管清洁剂 胶结强度
Keywords:
 well completion through tubing cement plug plugging casing cleaner cementing strength
分类号:
TE257
DOI:
10.19680/j.cnki.1004-4388.2020.04.006
文献标志码:
B
摘要:
 过油管打塞作业所形成的水泥塞长度较短,造成可靠性差、密封性不好,施工成功率相对较低。根据水泥塞封堵高压的原理,分析影响水泥塞胶结强度的诸多因素,以及造成施工成功率低的原因,通过配套使用膨胀式水泥和套管清洁剂,有效地改善了过油管打灰作业的封堵能力、可靠性,提高了作业成功率。在某国东部油田67口井的应用,成功率由895%提高到985%。该技术改进有效可靠,具有一定的市场前景和推广价值。
Abstract:
 The length of the cement plug formed by the plugging operation through tubing is relatively short, resulting in poor reliability,〖JP2〗 poor sealing, and relatively low operating success rate. According to the principle of the high pressure of the cement plug, the influencing〖JP〗 factors on the cementing strength of the cement plug and the reasons for the low operating success rate were analyzed. The combined use of expandable cement and casing cleaner can effectively improve the sealing ability, reliability and the success rate of the operation. The improved technology has been applied to 67 wells in an eastern oilfield in some country, and the success rate has been increased from 895% to 985%. The technology improvement is effective and reliable with certain market prospects and promotion value.

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备注/Memo

备注/Memo:
 2020-04-16收稿,2020-06-20修回,2020-07-01接受,2020-08-20网络版发表
刘飞,男,1980年11月出生,硕士,工程师,2019年毕业于中国石油大学(华东)石油工程专业,目前从事国内试油试气工作。电话:13643289206;Email:99769960@163.com。通信地址:河北省任丘市渤海钻探井下作业分公司,邮政编码:062552。
更新日期/Last Update: 2020-09-21