[1]肖志永,李超,刘皓,等.水力泵排液测试中的不压井作业技术[J].油气井测试,2021,30(04):26-31.[doi:10.19680/j.cnki.1004-4388.2021.04.005]
 XIAO Zhiyong,LI Chao,LIU Hao,et al.Snubbing technology in hydraulic pump discharge test[J].Well Testing,2021,30(04):26-31.[doi:10.19680/j.cnki.1004-4388.2021.04.005]
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水力泵排液测试中的不压井作业技术()
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《油气井测试》[ISSN:1006-6977/CN:12-1485/TE]

卷:
30卷
期数:
2021年04期
页码:
26-31
栏目:
出版日期:
2021-08-25

文章信息/Info

Title:
Snubbing technology in hydraulic pump discharge test
文章编号:
1004-4388(2021)04-0026-06
作者:
 肖志永李超刘皓刘喆焦金龙钱虎
 中国石油大庆油田有限责任公司试油试采分公司 黑龙江大庆 163412
Author(s):
XIAO Zhiyong LI Chao LIU Hao LIU Zhe JIAO Jinlong QIAN Hu
 Testing Branch, PetroChina Daqing Oilfield Co., Ltd., Daqing, Heilongjiang 163412, China
关键词:
 不压井作业 水力泵 排液 压裂 地层污染 产能 施工周期
Keywords:
 snubbing operation hydraulic pump drainage fracturing formation pollution capacity construction period
分类号:
TE358
DOI:
10.19680/j.cnki.1004-4388.2021.04.005
文献标志码:
B
摘要:
 高压油气井压井作业易造成地层污染,导致油气井在一段时间内难以恢复到施工前的产能状态,不利于油、气井求产。通过分析不压井作业工程参数,使用不压井作业设备下入水力泵排液测试管柱,只要压力在额定压力之内,即可进行不压井作业下水力泵排液。通过4井次不压井作业现场应用,及对2015年、2016年水平井施工动态数据的收集整理发现,使用不压井作业后,从钻完桥塞开始放喷至下完水力泵排液管柱的平均时间由904 h缩短至190 h。水力泵排液测试中的不压井作业技术可有效减少地层污染,缩短施工周期,是未来测试地层产能的发展趋势。
Abstract:
 The killing operation of highpressure oil and gas wells is easy to cause formation pollution and make it difficult for oil and gas wells to return to the preconstruction productivity state in a period of time, which is not conducive to the production of oil and gas wells. By analyzing the engineering parameters of snubbing operation, using the snubbing equipment to run the hydraulic pump discharge test string, if the pressure is within the rated pressure, the hydraulic pump discharge can be carried out under the snubbing operation. Through the field application of four wells of snubbing operation and the collection and collation of the dynamic data of horizontal well construction in 2015 and 2016, it is found that after using snubbing operation, the average time from the start of blowout after drilling bridge plug to the completion of discharge after run in hydraulic pump string is shortened from 904 h to 190 h. The snubbing technology in hydraulic pump discharge test can effectively reduce the formation pollution and shorten the construction period, which is the development trend of formation productivity test in the future.

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备注/Memo

备注/Memo:
 2020-08-26收稿,2021-05-29修回,2021-06-10接受,2021-08-20网络版发表
中国石油天然气股份有限公司科学研究与技术开发项目“气井带压作业技术推广”(2020B-4121(GF))
肖志永,男,1984年出生,工程师,2008年毕业于西南石油大学石油工程专业,现主要从事油气勘探开发和管理工作。电话:0459-5672042,13766784402;Email:xiaozhiyong1206@163.com。通信地址:黑龙江省大庆市让胡路区银浪乘南18街18号大庆油田有限责任公司试油试采分公司,邮政编码:163412。
更新日期/Last Update: 2021-09-14